"Vampire Taps"; and you had to be very careful and pedantic, to ensure that it was done properly. (A simpler version is available for making "live" connections to water pipes.)
Also the "Thick Ethernet" had markings about every 2.5 Metres; and you had to make sure that this was the minimum distance between adjacent taps, otherwise there could be standing/reflected wave problems.
I have fitted many of them; but one stands out, as it fed a particularly critical department.
As a result I had to climb a 25 foot, 4 part extension ladder, to reach the location up in the roof structure, carrying the required parts tucked in to my shirt and pockets.
No platforms etc, teetering and manoeuvring at the top of a shoogly (shaky and "buckling") ladder, two Works Engineering staff trying to steady it at the bottom; and because of it being in a "corridor", unable to get the ladder over to the best angle from vertical.
And being up in the roof - extremely warm.
The first operation was to fit a clamp, an essential part of the Vampire Tap Unit, on to the cable, making sure that all four Allen screws were properly bedded down, not trapping any insulation.
If even this "simple" operation was not done properly, the actual pointed tap, which was later screwed in to the clamp, would not fully penetrate the coax cable and reach the centre conductor.
In that aspect, all dimensions affecting the tap penetration were critical.
The next operation was to drill in to the cable, via the tap threaded hole in that clamp; but with a special, hand operated drill.
Basically a short drill bit about 1/4 inch long (6mm) mounted in a handle.
Generally the clamp and tap hole was on the far side of the cable, so one had to reach beyond that point, then bring the drill bit back towards oneself; but in that hole.
Then twist the drill etc anti-clockwise as viewed, pulling it towards oneself, hand and wrist bent at right-angles, to aid the penetration of the cable - generally the opposite direction to conventional drilling.
Making sure that the hole was cleared of swarf, the tap was fitted in to the clamp, again having to be fully screwed in to ensure the proper penetration to the inner conductor.
Mount the main body of the tap unit to the clamp, then strapping it in this case to the inverted L-shaped roof beam.
Connect up the drop cable, in this case a particularly long and heavy one; and strapping it to the beam at least twice, using three nylon straps to each strap group.
What would be the centre strap of each group was tightened on the beam alone first, placing the cable over/outside/not trapped by this strap, followed by the other two enclosing the drop cable, either side and as close to the centre strap as possible, thus forming a shallow "omega" in the cable giving extremely good retention.
Additionally, to help ensure good connections at the main tap unit, ensuring that the immediate part of the cable had some slack which was absorbed as some compression in to the tap unit.
This was done by ensuring that the leading edge of the shroud reached the main end face of the tap unit, tightening the two restraining straps in the first group, then pulling the cable connector back slightly, to offer up to and enter the corresponding connector on the tap unit, thus compressed or "forced in".
The second (and occasionally more) group of ties helped ensure that any subsequent minor movements of the drop cable would not affect the tap unit connections.
Wearily and warily descend the ladder, to connect the lower end of the drop cable to the Server, with its onward connections to the PCs or terminals; and ensuring that all were working correctly.
Make my way back about 1/3 mile (600 Metres), to resume my program writing, systems analyses, general trouble-shooting et al.
Also many a caper with Thin Ethernet and Appletalk.
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On another occasion when we had taken over another building, the local management insisted on employing a networking company to make 5 similar connections to a new, thick Ethernet cable, at about 7 foot (2.2 metres) above floor level etc and easily accessed,
I subsequently had to re-do four of them, basically the clamps had not been properly mounted, showing slack in the Allen screws, trapping etc, so all the rest of the operation suffered.
Edited by deleted (Thu 04-Sep-14 12:00:52)